Case histories with DP cell problems
Differential pressure
(DP) cells are the most often used level measuring device in the process
industries. Differential pressure cells measure the pressure difference between
two points and send a differential pressure reading to the plant control
system. Typically, DP cells are rated in inches of water equivalent. Standard
ranges include 0 to 20, 0 to 50, 0 to 100, 0 to 200, and 0 to 500 inches of
water differential pressure.
The control system
converts the DP cell reading into a liquid level based on an assumed specific
gravity inside the vessel. Levels based on DP cells can err for different
reasons. Previous columns have covered many reasons DP cells or sight glasses
can give false readings. This column covers some case histories of specific DP
cell problems.
Cryogenic unit with
two operating modes
The first case
involves a cryogenic field extraction unit that had two possible operating
modes. The first mode was an ethane rejection mode where ethane was sent
overhead. The second mode was an ethane recovery mode where the main tower
switched to a demethanizer operation. The overhead product was methane and
lighter and the bottoms product was ethane and heavier. The recovered liquid
(tower bottoms) was sent to a separate plant that segregated the liquid stream
into consumer LPG and petrochemical feeds.
The plant started up
in the ethane rejection mode successfully and operated there two years. After
downstream facility modifications were made, the plant shifted into the ethane
rejection mode. Tower problems occurred immediately. Major problems were
intermittent flooding of the tower and inability to effectively control cold box
heat integration.
Fig 1: Effect of improper liquid levels in overhead drum
Field troubleshooting
identified the culprit as changed densities in the tower. The ethane recovery
mode had lower liquid densities. The lower liquid densities inside the tower
caused 'measured' liquid levels to be lower than the actual liquid levels.
Normal tower boot liquid level variations caused liquid back-up into the
reboiler return line. Normal overhead drum liquid level variations (Figure 1)
created liquid entrainment into the overhead vapor going to the heat
integration in the cold box. The problem was especially acute in the overhead
drum.
Calibrating the liquid level measurement for the new
densities immediately corrected the operating problems.
Water hold-up causing
level problems in overhead reflux drums
Many drums in
hydrocarbon systems have water boots and separate water levels controllers.
Typical services that have these on overhead drums include atmospheric columns,
coker main fractionators, visbreaker atmospheric columns, and fluid catalytic
cracker (FCC) main fractionators, among others.
On one FCC main
fractionator, a fouled water level measurement resulted in pump cavitation,
seal problems, and increased maintenance costs.
Immediately after a
turnaround, the FCC started up without problems. However, after several weeks
of operation pump seal problems on the reflux pump became common. Field
troubleshooting quickly identified that the pump was cavitating. The initial
conclusion was that the net positive suction head (NPSH) available was
insufficient. This was puzzling because the pump had always worked before. An
alternate idea proposed at this point was that the pump was damaged, creating a
need for a higher NPSH. One pump of the two parallel pumps in the service was
pulled and inspected. No apparent reason for NPSH problems was found with the
pump. Design of the piping from the drum was checked. Again, no source of NPSH
problems was found.
Fig 2: Blocked water level taps
Over time, the new
operation was accepted as normal. However, the situation continued to nag on
some of the operators involved. While on site for operator training, the author
was asked about this problem and a new troubleshooting effort started. Field data
was gathered and compared to operating data. One suspicious observation was
immediately obvious. The water level measured in the drum never seemed to vary.
The connections to the water level instrument were blown out and the instrument
placed back in service. The measured water level immediately jumped from 54% of
range to 100%. The water level was above the upper water level tap. A plug in
the line to the water level instrument had blocked the instrument at 54% of
range.
Actual water level
varied down to nearly zero to up to the internal draw-off pipe to the
unstabilized naphtha pump. Two problems were damaging the pump. First, water
density is much higher than the naphtha density. The reported naphtha level in
the drum was much higher than the actual naphtha level. Calculations showed
that under some conditions the flow to the pump could be cut off entirely. At
other times water ended up in the pump suction. Sudden water slugs to the pump
dramatically increased power load and caused pump damage.
Review of operating
records showed that at the same time pump seal failures increased, gas plant
operation became less stable. The water in the unstabilized naphtha increased
water entrapment in the gas plant absorber-stripper and increased propylene
losses. The problems, seemingly unconnected, had the same cause, a single level
instrument giving incorrect readings. Supporting evidence came from trends in
main fractionator pressure drops. The main fractionator pressure drop had been
gradually rising. Water in the main fractionator reflux vaporizes inside the
fractionator and deposits solid salts. The salts plug trays and packing,
increasing pressure drop.
Unit operation
substantially improved with the level instrument back in service correctly.
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